Uart4是不是被其他模块占用了?
使用android7.1控制uart4的时候,发现波特率老是被修改为9600,是不是被其他模块占用了,要如何修改?
01-18 09:25:53.685 410 947 E u-blox: ubx_thread: read error 0
01-18 09:25:53.686 410 947 V u-blox: connectReceiver: Open/Reopen the serial port
01-18 09:25:53.686 410 947 V u-blox: CSerialPort::openSerial: Serial port opened, fd = 166
01-18 09:25:53.686 410 947 V u-blox: connectReceiver: Init receiver
01-18 09:25:53.686 410 947 V u-blox: CUbxGpsState::powerOff: placeholder for power OFF function
01-18 09:25:53.686 410 947 V u-blox: CGpsIf::gpsStatus: current GPS status: (still) 4 (GPS_STATUS_ENGINE_OFF)
rk3399的4G容量开发板
尝试wike如下修改还是不行
3.3 修改方法
3.2中的固件默认是支持GPS的,而公版固件默认关闭该功能。用户可以根据需要修改/system/build.prop里面ro.factory.hasGPS参数(false/true),实现禁止或者使能GPS功能,改完之后需要重启机器才会生效。
可以查看到ro.factory.hasGP已经修改为false了,但ttyS4操作时还是会失效,日志如下:
01-18 08:51:00.049 400 954 E u-blox: ubx_thread: read error 0
01-18 08:51:00.049 400 954 V u-blox: connectReceiver: Open/Reopen the serial port
01-18 08:51:00.049 400 954 V u-blox: CSerialPort::openSerial: Serial port opened, fd = 166
01-18 08:51:00.049 400 954 V u-blox: connectReceiver: Init receiver
01-18 08:51:00.049 400 954 V u-blox: CUbxGpsState::powerOff: placeholder for power OFF function
01-18 08:51:00.049 400 954 V u-blox: CGpsIf::gpsStatus: current GPS status: (still) 4 (GPS_STATUS_ENGINE_OFF)
可见,gps服务还是在工作
是否还要修改什么地方?谢谢! nila 发表于 2018-5-3 17:30
rk3399的4G容量开发板
尝试wike如下修改还是不行
3.3 修改方法
diff --git a/device/rockchip/common/ueventd.rockchip.rc b/device/rockchip/common/ueventd.rockchip.rc
index 95f9ed4..e6418dc 100755 (executable)
--- a/device/rockchip/common/ueventd.rockchip.rc
+++ b/device/rockchip/common/ueventd.rockchip.rc
@@ -48,6 +48,9 @@
/dev/accelirq 0660 system system
/dev/compassirq 0660 system system
#for GPS u-blox
+#/dev/ttyS4 0666 gps gps
+
# for GPS
#/dev/ttyS3 0600 gps gps
/dev/gps 0660 gps gps
diff --git a/device/rockchip/rk3399/BoardConfig.mk b/device/rockchip/rk3399/BoardConfig.mk
index 859c46b..af03d12 100755 (executable)
--- a/device/rockchip/rk3399/BoardConfig.mk
+++ b/device/rockchip/rk3399/BoardConfig.mk
@@ -70,4 +70,7 @@ BOARD_SENSOR_MPU_VR := true
//MAX-SIZE=2G, for generate out/.../system.img
BOARD_SYSTEMIMAGE_PARTITION_SIZE := 1610612736
# product has GPS or not
+BOARD_HAS_GPS := false
+
ENABLE_CPUSETS := true
同时将以上修改加上试试 加上以上修改后,还是会有相同的问题,波特率被修改回9600。出错时会有如下日志打印:
01-18 13:55:27.585 6031264 E u-blox: ubx_thread: read error 0
01-18 13:55:27.586 6031264 V u-blox: connectReceiver: Open/Reopen the serial port
01-18 13:55:27.586 6031264 V u-blox: CSerialPort::openSerial: Serial port opened, fd = 165
01-18 13:55:27.586 6031264 V u-blox: connectReceiver: Init receiver
01-18 13:55:27.586 6031264 V u-blox: CUbxGpsState::powerOff: placeholder for power OFF function
01-18 13:55:27.586 6031264 V u-blox: CGpsIf::gpsStatus: current GPS status: (still) 4 (GPS_STATUS_ENGINE_OFF)
是否应考虑将GPS的服务关闭?该如何操作?谢谢! nila 发表于 2018-5-3 19:48
加上以上修改后,还是会有相同的问题,波特率被修改回9600。出错时会有如下日志打印:
01-18 13:55:27.585 ...
device/rockchip/rk3399/gps/u-blox.conf
改这个文件 修改了device/rockchip/rk3399/gps/u-blox.conf这个文件,
修改为SERIAL_DEVICE /dev/ttyUSB4
这样log会一直打印找不到串口
01-18 08:58:35.757 5971273 V u-blox: connectReceiver: Open/Reopen the serial port
01-18 08:58:35.757 5971273 E u-blox: CSerialPort::openSerial: Cannot open serial port /dev/ttyUSB4, return -1 0
01-18 08:58:35.757 5971273 V u-blox: CGpsIf::gpsStatus: current GPS status: (still) 4 (GPS_STATUS_ENGINE_OFF)
01-18 08:58:35.757 5971273 E u-blox: connectReceiver: Failing to reopen the serial port
有没有办法可以完全关闭他呢?
谢谢! V/u-blox(462): ubx_thread: MSG UNKNOWN size 123 V/u-blox(462): ubx_thread: MSG UNKNOWN size 123
这是什么意思啊,是不是异常了
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